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Re: [Amps] 400 watt Polyfet HF amplifier

To: amps@contesting.com
Subject: Re: [Amps] 400 watt Polyfet HF amplifier
From: Manfred Mornhinweg <manfred@ludens.cl>
Date: Fri, 19 Jan 2018 18:04:45 +0000
List-post: <mailto:amps@contesting.com>
Hi John,

> Polyfet has a 2014 technical bulletin on their website, TB239.

Please allow me to throw a bucket (or at least a few cups) of cold water on that design:

- According to the gain curves shown, that amplifier is pretty linear up to a PEP of roughly 300W at 2MHz, 250W at 15MHz and 230W at 30MHz. The 400W rating is for deep saturation, not for linear service.

- The claimed efficiency of 66 to 70% is for the saturated condition, at 400W. Another graph shows efficiency at 1dB compression, and goes from 66% and nearly 400W at the low frequency end to 58% and 290W at 30MHz.

- The IMD is rated at 300W, and is barely -28dB for IMD3 at 16MHz. It's much better at the low extreme of the frequency range. And there is a reason for this...

- At 400W the rated IMD3 is clearly too bad for ham use.

Now some technicalities:

- The bifiliar feed choke is completely inadequate, having far too high leakage inductance. It acts like a bifiliar choke only at the low end of the frequency range, degrading effectively into two separate chokes at the higher frequencies, so that the two drains become uncoupled in that range, making the amplifier run in something close to current-mode class D rather than in class AB. This explains the drastic worsening of IMD as the frequency increases beyond the proper range of that choke.

- This bifiliar choke is drawn with the wrong phasing in the schematic.

- The bypass capacitors C11-C16 are poorly placed. The loop formed by the FET, the bifiliar choke, and these capacitors should be absolutely the shortest possible. It would have been easy to place them better.

- This amplifier has no common-mode feedback whatsoever, and almost no common-mode gate loading. Of course there is no common-mode drain loading either. For these reasons I would suspect that it is extremely prone to common-mode self-oscillation. This is an often overlooked problem in push-pull amplifiers.

And a minor thing: Strapping together the two cores of the output transformer isn't a clever thing to do. It would be better to leave some distance between them. Magnetically it makes no difference, but separating the cores gives a thermal advantage by exposing much more of their surface to cooling air.

After so many bad points, I would also like to stress a good one: This amplifier shows a good layout with the bifiliar choke soldered directly to the drain connections, and the output transformer shoved out of the way of the choke. Many designers don't get this right.

Manfred


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